![]() |
06-27-2011, 03:21 PM
|
#50866 |
|
Resourceful Weasel
Joined: Dec 2010
Location: Colorado Springs, CO
Oddometer: 99
|
Perhaps this is a weakening coil issue. I had a similar experience and it turned out the coil was weak and replacement with a new coil remedied the poor gas mileage.
|
|
|
06-27-2011, 03:42 PM
|
#50867 | |
|
All bikes are dirt bikes
Joined: Mar 2008
Location: Ottawa
Oddometer: 1,431
|
Quote:
the procycle screw is out 3/8 of a turn and the bike runs great. If I remember right, I can stutter the engine of I turn it in all the way. I will re-install the original and see what happens. All this time I thought my stock pilot jet was too big but didn't want to play with it right now.
__________________
And what are you planning to do with your one and only life? |
|
|
|
06-27-2011, 03:42 PM
|
#50868 | |
|
Southern Explorer
Joined: Apr 2006
Location: Jacksonville, Alabama
Oddometer: 1,233
|
Quote:
Are you sure the needle is clipped at 4 down from the top leaving two open slots below the e-clip? Is the spacer placed correctly below the shelf in the little recess? Double check your needle, is it layed out right? When I do a jet kit, I try and start with a good working stock set up. It must be very clean and in proper working condition. That needle and jet setting should be perfect at 2,000 feet MSL. Needle at 4 and the 145 main is what you use with a stock exhaust and cut air box. So, your jetting is not the problem.... If its just a rich loading up bog, its probably the needle or a float issue.. |
|
|
|
06-27-2011, 08:20 PM
|
#50869 |
|
Adventurer
Joined: Mar 2011
Location: west Michigan
Oddometer: 35
|
Baffle in stock muffler?
The stock exhaust on my '97 DR sounds kinda "raspy". I can insert a length of 1/2" TW conduit 17 1/2" into the muffler. I'm wondering if it may have been drilled.
|
|
|
06-27-2011, 08:21 PM
|
#50870 |
|
Studly Adventurer
Joined: Dec 2009
Location: Long Island, NY
Oddometer: 739
|
noob question
Noob question from a noob... Whats the small screw here do? It clicks and turns in and out, as if its an adjustment of some sorts...
__________________
2000 Suzuki DR650 - 790cc Big bore kit, V-Strom seat, Warp 9 Supermoto rims, TM-40 carb. 1985 Yamaha CA50 - My Hot Rod 2009 Piaggio BV-250 - Escusi, Babba be bo-bee |
|
|
06-27-2011, 08:35 PM
|
#50871 |
|
MacGyver
Joined: Jul 2009
Location: Canada
Oddometer: 1,973
|
That's the compression damping adjustment screw. Crank it in to increase damping when the shock is being compressed. There is no rebound damping adjustment.
If you weigh over 175 lbs, just turn it in all the way, or close to it.
__________________
_______________ "You can't put the shit back in the donkey." - Tony Soprano FYYFF
|
|
|
06-27-2011, 09:49 PM
|
#50872 |
|
Beastly Adventurer
Joined: Sep 2009
Location: SE Denver-ish
Oddometer: 2,551
|
Your hunch is correct, my stock pipe has a solid disk, 4-3/8" in. Now, I'd mention that although it's stamped US Forest Approved Spark Arrestor (or there-a-bouts), if a ranger sticks a rod in there, you might be screwed.
|
|
|
06-27-2011, 10:40 PM
|
#50873 |
|
Gnarly Adventurer
Joined: Feb 2011
Location: Oregon (The valley)
Oddometer: 233
|
Nice Ride...
Over the weekend, I got a chance to do a little camping and riding the DR up some logging roads. It was lots of fun, just was a bit "squirrely" with the trail tires on the gravel.
![]()
__________________
2006 DR650 Oregon Tag-O-Rama ![]() http://www.advrider.com/forums/showt...=752387&page=3 |
|
|
06-27-2011, 10:49 PM
|
#50874 | |
|
n00b
Joined: Apr 2008
Oddometer: 5
|
Quote:
|
|
|
|
06-28-2011, 12:10 AM
|
#50875 | |
|
fNg
Joined: May 2011
Location: Rancho Cucamonger, CA
Oddometer: 779
|
Quote:
bottom the screw out carefully and run it back out 8 turns. that's the factory setting (IIRC) adjust from there. i run mine 2 clicks in for twisties and 1 click in for normal street. for the trail play with the settings.
__________________
2006 DR650SE, daily commuter + a StripleR and a bunch of 2 strokes that you dont want to read about. :) http://www.advrider.com/forums/showthread.php?t=829203 |
|
|
|
06-28-2011, 03:36 AM
|
#50876 | |
|
Procrastinators
Joined: Mar 2008
Location: Near Ottawa, ON, Canada
Oddometer: 5,787
|
Quote:
Manual says stock setting is 8 clicks out. Actually, I just checked and it says "8 clicks turns out", so that's clarified the issue. ;)
__________________
Want to know more about the Garmin Montana? See the Wisdom and FAQ Thread. "Don't play a lute to a cow" (Old Chinese Idiom) "The motorcycle, being poorly designed for both flight and marine operation, sustained significant external and internal damage," police noted. |
|
|
|
06-28-2011, 03:46 AM
|
#50877 | |
|
MacGyver
Joined: Jul 2009
Location: Canada
Oddometer: 1,973
|
Most people will agree that if you're 150 lbs or less, then the stock shock isn't so bad (in terms of spring rate, at least). At the same time, everyone agrees that the shock is grossly under-damped. And the lack of rebound adjustment doesn't help.
Anyone over ~ 180 lbs or so has surely considered re-valving the shock to improve damping and replacing the spring with something a little stiffer. Yes, setting the adjustment screw to 8 turns (or whatever the factory setting is) is a good starting point for many but most people will end up with the screw all the way in when they're finished, or very close. Quote:
__________________
_______________ "You can't put the shit back in the donkey." - Tony Soprano FYYFF
|
|
|
|
06-28-2011, 03:48 AM
|
#50878 |
|
Gnarly Adventurer
Joined: Nov 2007
Location: Asheville, NC
Oddometer: 267
|
Played with my carburator more last night. None of the tubes are kinked and the boots are on tight but I still get a bad bog. I tried raising the e clip (lowering the needle) to the 3rd notch instead of 4th but still get the bad bog. The e clip is setting down under the shelf and the d shapped washer is also in line with the shelf. I played with the fuel screw and it will kill idle when turned all the way in. Its out at about 1 1/2 turns right now but surely that adjustment wouldn't cause this kind of bog. I've taken out the filter in the inlet to the carb to make sure that wasn't it. I'm sure I've screwed something up but I just can't figure out what.
2009 DR650, procycle jet kit, stock exhaust, cut airbox, 145 main. |
|
|
06-28-2011, 05:07 AM
|
#50879 |
|
mc caregiver
Joined: May 2007
Location: Garland, Texas
Oddometer: 2,586
|
|
|
|
06-28-2011, 05:33 AM
|
#50880 |
|
misadventurer
Joined: Oct 2007
Location: Johannesburg, South Africa
Oddometer: 552
|
Silverwolf - also check that the little vacuum tube running from the top of your carb isn't dipping into the airbox. Also ensure it's out of the airstream. I tucked mine behind the side cover.
As noted by others - check the float. Make sure your boots are all seated properly. Check also that the slide is ok. Maybe do a teardown and reinstall. You'll get it dialed in.
__________________
Plans to get my own piece of paradise (comments and advice welcome): http://mountain2c.wordpress.com/ jenx screwed with this post 06-28-2011 at 06:05 AM |
|
|
![]() |
| Share |
| Thread Tools | Search this Thread |
| Display Modes | |
|
|